Productivity improvement as a facilitator of reshoring and growth at small companies A case study in the Swedish electronics manufacturing industry
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Publicerad
Författare
Typ
Examensarbete för masterexamen
Master's Thesis
Master's Thesis
Modellbyggare
Tidskriftstitel
ISSN
Volymtitel
Utgivare
Sammanfattning
The Swedish electronics manufacturing industry has faced significant competition from
countries with lower labour costs, resulting in production being relocated. However, at some
companies, there is a growing interest to bring back production to the country of the company.
To remain competitive, companies need to constantly improve productivity. At the luminaire
manufacturer in this case study, having more production in Sweden would make it easier to
fulfil customer demands, but the cost of producing locally is currently too high to make it
feasible. Therefore, this thesis aims to investigate the potentials for improving the productivity
at the company.
The first part of the thesis was investigating if insights could be gained from the data in the
surface mounting technology (SMT) production. Then, the second part was understanding the
current situation in the luminaire assembly and suggest improvement. A combination of
qualitative and quantitative methods was used to achieve this. Interviews and observations,
including participation, were used to gain an understanding of the products, material flows
and work processes. Then, machine data, ERP data and time studies allowed the theoretical
and actual production times to be analysed, allowing productivity improvement potentials to
be found.
In the SMT production, data was found for theoretical and actual cycle times. By comparing
these, key performance indicators (KPI) like availability and performance could be
determined. This indicates that a better system for handling the data could be very valuable.
In the assembly, many potentials for improvement were found. The proposal still includes preproduction in China, but all units of the product in the case are to be finished in Sweden.
Then, the material flows could be changed with, among other things, a kanban system.
Finally, by moving tools and materials closer to the operator at the assembly station, as well
as providing them with support and standardization, the time for assembling the product could
decrease by 30-50%.
Beskrivning
Ämne/nyckelord
Productivity, Manual assembly, Material flow, Improvements, Sequential activity and methods analysis (SAM), Work design
